S
SurfnSun
Guest
Well I spent a good portion of my day today down at Norris Motorsports. Frustrating.
There isn't really much good to report.
We ran the car and tried to adjust the Microfueler. No luck.
I told Mike about my conversation with Sam, and we put a vacuum gauge on it. It wasn't holding vac. There is a weird conglomeration of brass T's in the vacuum line off of the plenum. We pulled that mess off and simplified it a bit and attatched new vac line. Put the gauge back on it, and it held pretty well, there a very very minimal leak down. Ran the car again, it got better. There is still two spots where the A/F spikes lean and causes a serious studder in power. I can't remember if the last run was made with the "fat" chip or not.
Another disappointment was my #s. Mike must have been thinking crank tq when he gave me my rwtq number. It wasn't 550
It was around 490rwtq. which would give me 555tq at the crank. Though when this issue gets straight is should be over 500rwtq. Hp was just a few below 400, and will exceed that when the lean out is solved. However, the car was so hot you could cook a 5 course meal on the intercoolers. I could feel the heat from 12 ft away, that probably hurt my numbers a bit.
Anyway thats my day. It was cool to see my car again, and hear the turbos spool up on the dyno. I just wish we could get it fixed.
Thanks again Sam.
There isn't really much good to report.
We ran the car and tried to adjust the Microfueler. No luck.
I told Mike about my conversation with Sam, and we put a vacuum gauge on it. It wasn't holding vac. There is a weird conglomeration of brass T's in the vacuum line off of the plenum. We pulled that mess off and simplified it a bit and attatched new vac line. Put the gauge back on it, and it held pretty well, there a very very minimal leak down. Ran the car again, it got better. There is still two spots where the A/F spikes lean and causes a serious studder in power. I can't remember if the last run was made with the "fat" chip or not.
Another disappointment was my #s. Mike must have been thinking crank tq when he gave me my rwtq number. It wasn't 550

Anyway thats my day. It was cool to see my car again, and hear the turbos spool up on the dyno. I just wish we could get it fixed.
Thanks again Sam.
